FLA-LSCSE
August 28th, 2000, 08:21 PM
Well I finished installing the GT-40 intake tonight and also the ported heads.About 16 hours by myself...6 of which went into the porting work...Now the real fun begins.I have and had a few problems.
1.)Had an electrical fire at the starter solenoid...minor but it was actually a good thing as I FINALLY found my short circuit that was killing my battery.
Had to do a little(8 wires)rewiring but it is fixed.
2.)Upon firing the engine I could not get the engine to idle at all. I ended up pulling a vaccuum line and the engine will idle but horribly.I kept trying to find the source of the problem and found that the MAP sensor did not have a vaccuum line to it. So I added vaccuum and the idle quality immediately improved but still sucks sweaty goat balls. The engine is running now with a very BIG vaccuum leak(intentional mind you)in order to keep it running.The engine is so rich it will fry your eyes out.It seems to be running on the O2 sensors only.I have double checked every wire and connection to see if I missed something.As it stands now it sounds like I have a BIG cam in it.It runs and is very fast now but it loads up.
I am not sure where to even look for the answer so ANY help will be appreciated.
BTW I posted some photos of the swap on my site as well as some pics of the porting job. Gerry from B.I.C. did an excellent job on them!
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Dave
http://tnmotorsports.com/lsc/lsc.htm
[This message has been edited by FLA-LSCSE (edited August 28, 2000).]
1.)Had an electrical fire at the starter solenoid...minor but it was actually a good thing as I FINALLY found my short circuit that was killing my battery.
Had to do a little(8 wires)rewiring but it is fixed.
2.)Upon firing the engine I could not get the engine to idle at all. I ended up pulling a vaccuum line and the engine will idle but horribly.I kept trying to find the source of the problem and found that the MAP sensor did not have a vaccuum line to it. So I added vaccuum and the idle quality immediately improved but still sucks sweaty goat balls. The engine is running now with a very BIG vaccuum leak(intentional mind you)in order to keep it running.The engine is so rich it will fry your eyes out.It seems to be running on the O2 sensors only.I have double checked every wire and connection to see if I missed something.As it stands now it sounds like I have a BIG cam in it.It runs and is very fast now but it loads up.
I am not sure where to even look for the answer so ANY help will be appreciated.
BTW I posted some photos of the swap on my site as well as some pics of the porting job. Gerry from B.I.C. did an excellent job on them!
------------------
Dave
http://tnmotorsports.com/lsc/lsc.htm
[This message has been edited by FLA-LSCSE (edited August 28, 2000).]