The rear of my '89 Mark VII LSC wouldn't
settle, which I traced to an inoperative
compressor relief valve. Upon discovering
the valve was not available separately
but only in an expensive new or rebuilt
compressor assembly, I worked out
the following inexpensive fix.
As of early 1999,
McMaster Carr (a
very large industrial supplier) is now online and sells to
individuals. In their catalog # 102, page 1653, there is a
"High Efficiency Miniature Air
Valve" (part # 62095K11) that
sells for about $20. It's 12 volt
dc, uses only 1.3 amps, and is very
small. The specs say it is good for
0° F to 120° F. It has push-in ports
to connect 5/32" truck airbrake
plastic air line. Any large truck
dealer will have this air line, it's
just a few cents per foot (you need
2 feet). From the truck dealer also
get a Weatherhead brass fitting;
you need a 90 degree compression
street ell, 1/8" pipe size,
for 5/32" plastic air line tubing,
and it has an inner tubing support
so the compression fitting won't
crush the plastic air line.
I installed a rebuilt dryer, which allowed me to cut apart
the old one to see how it is built. Drill an 11/32" hole in the very top of the side of the
dryer, in the thick part, which will put the hole well above the desiccant pellets
inside. Drill on the rear side, just to the inner fender side slightly from straight
back. Tap with 1/8" pipe tap. Wrap the brass fitting threads
with Teflon tape and screw into the drier. Point the fitting
toward the fender. I installed the air valve, with the ports
and wiring pigtails pointing toward the rear, behind the battery
on the inner fender to avoid the worst of engine bay heat.
Drill 2 small holes in the inner fender and use 2 small sheet
metal screws to mount the valve. I fashioned a protective cover
out of a small plastic bottle, positioned with one edge down,
and cut out the bottom edge for air circulation. Thread the
plastic airline under the top air dryer bracket, and connect
between the brass fitting and the valve. Clip the wires going
to the original relief valve close to the compressor. Solder
and heat shrink these wires to the pigtails on the new valve.
On my 89 Mk VII, the green wire goes to the black pigtail and
the blue wire to the green pigtail. I found the wiring diagram
for my car in a large motor manual in the local library.
I live in MO where we have occasional below zero weather and considerable heat
and humidity in the summer. I have had this on my car for over a year without
a single problem.
UPDATE: Current as of August
2004 -
This is some new info I developed recently while helping someone find materials
to install a remote relief valve instead of buying a complete compressor assembly.
The valve in the original article used 5/32" airline and
fittings, which have become somewhat difficult to find.
The valve comes from
McMaster Carr and
anyone can buy direct over the internet from them. That valve
now goes for about $27.00. (See original article above for
page and part #) The airline is available also from McMaster
Carr. Page 93, part # 62095K11, "DOT Nylon 11 Tubing",
available in a 5' length for 39 cents per foot.
There are several choices for fittings, also from McMaster Carr. All listed are
90 degree fittings. Straight ones are also available.
Page 136, 5/32"OD tube to 1/8" pipe adapter, Part
51055K44, good to 158 deg F, $2.58.
Page 145, brass fitting, part 51495K232, good to 175 deg F, $2.97.
Page 147, brass fitting, part 5523K32, good to 250 deg F, $3.44.
Another somewhat cheaper alternative valve would be on page
395, called a "Polypropylene
Direct-Acting Miniature Solenoid Valve"
It's 12 volt dc with 1/8" female
pipe fittings which would allow it
to be used with very commonly available
fitting and plastic airline sizes,
like 1/8". It's available with
either 18" wiring leads or spade
connectors and is only around $18.00.
Part # 7877K25 or 7877K55.
I have also realized something else since I did mine. The drier is self-renewing.
It absorbs moisture as air is pumped to the bags. When the dry air is exhausted
from the bags, the system is designed so that the dry air passes back through
the desiccant and removes moisture. This way the desiccant does not become rapidly
saturated.
After realizing this, I moved my remote exhaust airline from the top of the drier
to the bottom, to allow the dry air being exhausted to pass through the desiccant
and absorb moisture. To keep the desiccant pellets from clogging the small airline,
I pushed a small wad of coarse steel wool into the hole before screwing in the
fitting.
Although the body of the drier is not as thick near the bottom, it held for me
for over a year with no problem. However, to be on the safe side I roughened
the outside of the drier body with coarse sandpaper around the fitting and applied
some epoxy adhesive to give a little added strength.