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351 WINDSOR SWAP (1989 MARK VII LSC)
Submitted by macx / 10-14-05



Introduction


This car is relatively heavy at 4,000 lbs and, with the stock 302 HO and high-first-gear ratio AOD with the very low stall stock converter and 3:27 gears, was weak on throttle response and especially low rpm torque both in town and on the open road in climbing hills and passing. (Beefed 4R70W & 2800 stall on the way, 3:55’s already in)

Having owned some serious muscle in bygone days, I yearned for more “under the loud pedal.” The car needed more power and torque so it’s performance would match it’s visual image – which I happen to think is still cool and definitely unique from most go-fasters, not to mention it’s a great road car with all the bells and whistles.

I got the opportunity to buy a 30k mile 95 Lightning roller shortblock which I preferred because of the capability of using a stock type roller cam and hardware, and it has the Ford heavy duty “football” rods and dished hypereutectic pistons which would work well with my intended compression ratio of around 9-1 and withstand some horsepower upgrades. It came with the required 351 EEC-IV distributor, and as it was originally a serpentine belt motor, the damper and crank pulley lined up with the front accessories from the 302. It had no sign of a cylinder wall ridge, so I just freshened it up with new moly faced rings, bearings, double roller timing set, oil pump (the existing pump had nicks in the gears), and heavy duty oil pump drive shaft. The cam bearings were fine. I took all the galley plugs out, gave the entire block including the cylinders and galleys a thorough cleaning and oiling, and reassembled the stock shortblock. Being on a very tight budget, I could not afford to get the block machined like I would have liked. That has to wait till it’s 393 time.

That budget also prompted me to gather parts over time, shopping for good used parts or new parts leftover from someone else’s projects at reduced prices. I was able to find nearly all major parts good used or leftover. The major new parts included the shortblock rebuild parts as listed above plus new ARP headbolts, all new sensors as the old ones had over 225k miles, plus of course gaskets. I also sprung for a new high performance water pump, high flow thermostat, Ford blue silicone hoses – all of which fit except the bypass hose was too short – new high performance cap, rotor and wires, roller cam gear for the distributor, stainless bolts for everything external, and the 351 balance flexplate. I got cheap chromed steel valve covers that were a little taller to clear higher lift rockers, plus a new throttle body and EGR plate at Ebay, and found a Trick Flow oil fill that fit the grommet hole in the valve cover and had the fitting for the tube to the EGR plate. Overall I figured about a 40% saving over new.

Virtually everything else was good-used or leftovers, from the swap pan and pickup, 1.9 intake Edelbrock Performer pedestal heads (3k miles for $600) which boosted the stock Lightning compression ratio from 8.8 to about 9.2, 1.72 Ford/Crane roller rockers to boost lift from .444 to .477 to compensate for the additional displacement, the hydraulic roller cam (a stock 302 HO cam as it had the desired .050 duration for a streetable power curve and torque peak, plus it was only $40 nearly new), the roller lifters and hold- down hardware, the intake, the headers, the mass air meter and injectors. My sources for the more critical parts like injectors, cam, rockers, etc, were the classifieds on www.corral.net and www.stangnet.com. I trusted eBay sellers for non-critical, non operating items like valve covers and other small items.

UPDATE: After driving the car for several thousand miles, I came to the conclusion that the Mustang guys were certainly right about not using too small a cam even in a relatively mild 351. Still trying to live within some kind of budget, I opted for a Trick Flow cam, just the Stage 1. It's 220 @ 050and around .500 lift with stock 1.6 rockers. I made some inquiries and was told that it would probably still clear my pistons with my1.72 rockers, which also upped the lift to .538 & .548 - to a non-Ford person that sounds like quite a lot, but I'm becoming a believer that we have to think differently than the other guys.

The valves cleared with room to spare. It idles just a tad rough (sounds nice!) but does idle steadily at 800. The seat-of-the-pants-o'meter showed a marked improvement in power across the board and I was amazed at getting an honest 24 mpg on a long road trip thru hilly terrain at nearly 80 mph with a severely loaded car.

Would have been fun to go to the Stage II, but I'm sure that would have overmatched my heads, intake, and compression ratio, and it really does scoot pretty good from a punch at any rpm and at any speed. And I am sooo happy with the mileage!

AND it's a bargain compared with other big name brand cams.





Parts You Will Need

I’ll now go through items that needed attention to complete the swap.

As I said, my shortblock was originally equipped with a serpentine belt setup, and came with the right damper and crank pulley so I didn’t need the pulley and spacer otherwise needed for a v-belt engine.

The passenger side accessories bolted right up, although the alternator ended up higher. This posed a problem with the radiator hose which, in this car, normally runs over the top of the alternator. I solved this problem fairly simply by cutting the radiator end off of another good hose back beyond the second curve and splicing it onto the end of the new hose with two clamps and a short length of exhaust tubing. That gave me enough length and the right curves so I was able to route the hose behind the alternator and around the passenger side of it. There’s a picture of it HERE.

The driver side accessories were a whole different matter. I don’t know if the stock Lincoln PS/AC bracket is different than a Mustang bracket, but I absolutely couldn’t figure out how to make the Ford 351 adapter bracket work. There were probably simpler ways to solve it than what I did, but I ended up with a bracket from an early 90’s 351W pickup. That positioned the PS pump a little closer to the battery, but it did clear. The AC bracket part of it took a different style compressor than my '89, so I had to fabricate an adapter. It also positioned the compressor high enough so I had to cut away a little bit of an underhood brace, besides removing more of the insulation.

The front cover and water pump from a 302 will fit a 351, but as I mentioned I went with a high flow pump. I learned that the water pump and front cover from pickup Windsors will also work, but you have to have the matching front cover to go with the pickup water pump as the passages where the two meet are different than for a car setup.

I used new stock Lincoln Mark VII motor mounts, which are the same as Fox Mustang convertible V8 motor mounts. They’re stronger than Mustang coupe mounts and position the motor a little bit lower, which turned out to be critical for hood clearance.

I had to get a 351 Fox swap double hump oil pan and pump pickup – Ford only makes a 5 quart swap pan. I understand there were some cars with 351s and that type of pan, maybe Crown Vics circa 1990 (?) The only thing to note with that pan in the Mark VII chassis is that the front swaybar hit the front drain plug. I put about 1-1/2” spacers with longer grade 8 bolts between the bar mounts and the frame which dropped the bar just enough to clear.

For intake, I found a GT40-351 lower that I mated to an early Explorer upper which is essentially the same as a Cobra intake. Other options would be to use the upper from i.e. a 302 Edelbrock Performer on their 351 truck lower, or a complete Trick Flow 351 intake, or to use a complete Cobra or Explorer intake adapted to the wider engine with either the Weiand (Holley) spacers or the better but more spendy ones from www.pricemotorsport.com. Using a stock 302 HO intake would excessively choke even a mild 351. Use of either of the other choices would depend on the performance level of the engine. As I targeted low and mid range torque, my low cost combination does just fine. I port matched the lower to the heads, and both the lower and upper to the plenum gasket. The lower was close, the upper I had to port out as much as about 1/16” in some spots. That was easily done with a sanding roll and drill motor. I transitioned the ports up about 1” into the runner. I didn’t use any plenum spacers as there was no under hood room to spare at all. I just went to the local building supply for the long center bolts that hold the plenum to the lower intake. I used cadmium plated (bright, shiny) so they wouldn’t rust and looked much like the stainless bolts I got for the rest of the exterior of the engine.

For hood clearance, I had to cut away a lot of the thick underhood insulation mostly in the center of the hood, as well as snipping out or pounding in some portions of the underhood bracing over the intake, throttle body/EGR plate, and the AC. Not very neat or professional, but I had a very limited time to get the car running.

I found a used set of shorty 351 swap headers that were ceramic coated. I decided on shorties strictly because I didn’t have the time to modify the front of the H-pipe to use long tubes. I figured I gave up maybe 10 or so hp and torque, but as this isn’t a radical engine, it was worth the reduced effort and cost. However, the headers were JBA brand and there were definitely some problems with them. I had to grind out quite a bit of excessive weld where the tubes were welded to the port flange plates as the weld intruded into the tube and would have caused turbulence and restricted flow. By far the worst problem was the fact that the collectors didn’t at all fit the front of the H pipe. They were in the right location, they were just angled wrong.

I luckily have a wire feed welder with which I was able to reweld the H-pipe flanges after cutting them off and reattaching them at a different angle using some wedge shaped inserts to fill in the gaps. I like the ceramic coating to prevent rust and reduce underhood heat, but I would not recommend the JBA brand! It was a very difficult, time consuming, and frustrating modification job that shouldn’t have been necessary.

The tube that goes by the steering shaft had a factory indent in it, but it was insufficient clearance on the Lincoln. I don’t know if it would have cleared on a Mustang. I massaged it inward a little bit more, but it still rubbed lightly when I got the header on. The header bolts toward the rear were difficult to access even though I used bolts with smaller than normal heads, so I didn’t want to go through removing the header to work the tube more, plus I didn’t want to dent the tube in more and further restrict the flow. It was much quicker and easier to get Mustang poly offset rack bushings. Instead of positioning the offset to raise the rack, I set the offset to move the rack toward the driver side (about 1/8”) which moved the rack and therefore the shaft just enough to clear the tube. The only little problem was that the steering wheel was then off center just a little, which I corrected by adjusting both tie rods. This then required an alignment. I had to jack the motor up so I could get the rack off of the mounting bolts to install the back half of the bushings. I discovered that also made the power steering hose connections on the rack MUCH easier to access. I also discovered the rack just cleared the pan, and I could not have used the offset bushings to raise the rack to correct bumpsteer as is the normal use for them. That probably was the result of using the lower Mark VII / Mustang vert motor mounts.

I was pleasantly surprised when I found that the large Lincoln brake and ABS assembly did not interfere with anything. In fact, I was able to mount the headers on both sides rather easily even with everything underhood in place. It was just the bolts that were hard to get at toward the rear of both headers. On the passenger side, I simply had to move the air pump hose hanger on the inner fender strut tower upwards a few inches to hold those hoses up and away from the headers.

To fit the air injection tube to the back of the heads, I had to cut the tube in the straight section behind the intake and use a 6” length of ¾” high temp silicone heater hose to widen it. The tube interfered with the AC drier bracket by just about ½” where it goes around the back of the passenger side head. Being in a hurry and with my AC not working anyway, I simply removed the drier and the tubes and hoses and the condenser in front of the radiator. The bracket or the tube will have to be slightly modified to be able to remount the drier and reinstall everything.

I had converted the car from speed density to mass air before I did the engine swap to make sure the system worked and to minimize the number of possible problem sources in case it didn’t. I got a cheap cold air intake setup off eBay.

I put all new sensors on the engine as all my original ones had high miles. For the intake air temp sensor, I drilled a hole in the metal intake tube in the curve just ahead of the throttle body and used a simple rubber grommet in the hole that fit tightly around the sensor. I extended the wires from the stock position in the manifold base at the front of the driver side. That got the sensor away from the exhaust gas stream let into the intake by the EGR and the resultant sticky carbon buildup which can’t do it any good.

The 302 fuel rails were adequate for my horsepower level and did fit that manifold complete with the pressure regulator. I understand they flow enough to support upwards of a high 300 horsepower range. They did have to be widened to fit the wider 351. I cut the very hard plastic crossover hoses off of the front and rear and used longer sections of efi specific high pressure fuel hose. It’s also important to use efi specific fuel hose clamps with rolled edges to avoid cutting into the hose. NAPA and I’m sure other places have them.

I also had to modify the hard heater transfer tubes that mount along the passenger side of the intake. I cut the little bracket that holds them together near the front and was able to install the one that hooks to the hose from the water pump. I had to cut and extend the other one with heater hose, and rebend some of the exiting bends to make it fit up to the front manifold water fitting. (Why couldn’t Ford make it simple and make the same tubes fit both 302 and 351 Windsors?!)

As the stock 351 EEC-IV distributor had a flat tappet drive gear on it, I had to change to the Ford “yellow stripe” roller cam gear. The gears are pressed on, and it was quite a challenge getting the old gear off and putting the new one on. The correct height for the gear has to be determined and the gear pressed on to that point on the shaft. Both the gear and shaft then have to be drilled for the tiny roll pin. I have a drill press but it was still difficult to get a good straight hole as the gear and shaft material are quite hard and the tiny drill bit flexes. If I had to do it again, I would take it to a good auto machine shop. I would also look for a light truck distributor that had the tfi module remotely mounted in a separate small plug that mounts up by the radiator rather than on the distributor where heat can make it fail. There’s a short wiring harness with plugs that connect the module to the distributor that you would also need.

As 351 blocks are taller, they also need different pushrods. My heads happened to have the stock style pedestal rocker arm setup which is much more difficult and time consuming to properly adjust than stud style rockers. HERE's how I did mine.

Proper pushrod length is important to get the proper travel pattern of the rocker tip on the valve stem. Both Crane and Comp Cams have good instructions on their website, and can provide pushrod length checkers that make the job much easier. I was, however, amazed to learn that Ford actually makes pushrods for 351s with Edelbrock Performer pedestal heads! One of these is where I found them (I think, if I remember correctly - not easy to find): www.buyfordmotorsport.com, www.nthcoast.com, www.parts123.com, or www.genuine-ford-parts.com, or just Ford Racing or a Ford high performance parts dealer should be able to find them.

I also needed a longer serpentine belt. To measure the length, I used a dressmaker’s cloth tape measure wrapped around the pulleys in the same manner as the belt.



I believe that covers almost every little detail. Ford being Ford, they of course don’t make it as easy or as relatively less costly as Chevy or Mopar to swap to a larger small block, but it can be done.

Here are links to some good references, some with part numbers etc. The main reasons I opted to go 351 and put up with the extra expense and difficulty was that a 351 in a Fox is more “unique” than a 302 stroker, the block will support more power “just in case” of future major power increases, and mostly because it can be stretched to much larger displacement than a 302 (besides, I’m stubborn!). In fact, all that is required for a basic 393 is a relatively inexpensive ~$250 cast crank and stock dimension 302 pistons hung on stock dimension 351 rods. That’s one of the reasons I snapped up the Lightning shortblock as it has the stronger stock “football” marine rods that only need basic rebuilding plus ARP rod bolts to hold some pretty serious power. ARP main cap studs and even a main cap girdle would be good additional insurance depending on the power level built into the engine. For that level combo, I would look at Speed Pro hypereutectic or forged pistons with the skirt coating which reduces piston and cylinder wall wear especially on the thrust side, and which are relatively inexpensive for the power they’ll hold.

Those points aside, it’s been pretty much proven that especially a 347 or even a 331 stroker 302 built with the same heads/cam/intake level will out accelerate a 351 mainly because of the lighter reciprocating assembly, and that such a motor will not cost any more to build and will be easier to accomplish than swapping in a built 351.

But I’m planning ahead to making mine a 393 with bigger heads/cam/intake for a Factory Five cobra replica – complete with beefed 4R70W automatic (yes!) for ease of driving in town and sneaky stoplight getaways in my (hopefully) golden years.

For now I’ve got gobs more torque and throttle response and am still getting 21.5 mpg at 2500 rpm / 78 mph. Life is GOOD!



Victory Hath Its Rewards!



- macx


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